StillSmart Home distillation made easy! 2012-11-14T15:18:57+00:00 http://www.stillsmart.co.uk/forum/feed.php?f=11&t=762 2012-11-14T15:18:57+00:00 2012-11-14T15:18:57+00:00 http://www.stillsmart.co.uk/forum/viewtopic.php?t=762&p=10599#p10599 <![CDATA[Re: Extension and Operation]]>
I have also made a Boka LM condenser which mostly relegates the Super Reflux to pot mode for stripping runs.

Statistics: Posted by Keystone — Wed Nov 14, 2012 3:18 pm


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2012-01-22T15:29:57+00:00 2012-01-22T15:29:57+00:00 http://www.stillsmart.co.uk/forum/viewtopic.php?t=762&p=6940#p6940 <![CDATA[Re: Extension and Operation]]>
I tend to use this link as a crutch. http://www.homedistiller.org/reflux_calc.htm
It helps estimate speed and when to quit.

Operation:

1. use the full 1380W to come to boil.

2. when the upper 3/4 mark of the extension feels warm, the bottom half feels hot and the top quarter feels less cold than the start; drop power to 750W and start cooling water.

3. maintain total reflux for a half hour at 65C while adjusting power as necessary.

4. raise power to 800 to 815W to slowly take off 50 ml of foreshots (to discard) and then the heads (some of which with a less estery smell may be saved to recycle).

5. keeping power under 825W will allow for compression of heads at 77C or just below.

6. collect heads in smaller lots such as 50 to 100 ml until cut to hearts.

7. upon cut to hearts, raise power to 950W - 1000W for a fast drip at 78.2 to 78.3C.

8. collect hearts in 200 ml lots.

9. when the purity remaining in the charge is 2% based on the calculation from the "crutch" link, collect output in 50 ml lots as tails will be imminent.

10. stop collection upon reaching 78.4C or sooner when output transitions to a rancid smell (discard tails with more than a hint of wet dog or wet cardboard).


Following these steps, a 17 L charge at 10% took seven hours from switch on to switch off. The result averages around 92%.

Statistics: Posted by Keystone — Sun Jan 22, 2012 3:29 pm


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2012-01-04T22:44:42+00:00 2012-01-04T22:44:42+00:00 http://www.stillsmart.co.uk/forum/viewtopic.php?t=762&p=6755#p6755 <![CDATA[Re: Extension and Operation]]> Statistics: Posted by Keystone — Wed Jan 04, 2012 10:44 pm


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2012-01-03T18:31:14+00:00 2012-01-03T18:31:14+00:00 http://www.stillsmart.co.uk/forum/viewtopic.php?t=762&p=6736#p6736 <![CDATA[Re: Extension and Operation]]>
If you are concerened about the soldering here is an alternative; copper ferrules that shouild be no more difficult to solder than a standard plumbing joint.

http://artisancopperworks.com/shop/article_1/2%22-Easy-Flange.html?shop_param=cid%3D3%26aid%3D1%26

I do not know what continent you are on, or what pipe the ferrules are designed to fit but a quick note to these very helpfull distillers should quickly sort out any interface problems.

Statistics: Posted by YHB — Tue Jan 03, 2012 6:31 pm


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2012-01-03T17:22:36+00:00 2012-01-03T17:22:36+00:00 http://www.stillsmart.co.uk/forum/viewtopic.php?t=762&p=6735#p6735 <![CDATA[Re: Extension and Operation]]>
If the ferrule does not need persuasion to fit. Then, solder prep must be done in addition.

Statistics: Posted by Keystone — Tue Jan 03, 2012 5:22 pm


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2012-01-03T15:45:11+00:00 2012-01-03T15:45:11+00:00 http://www.stillsmart.co.uk/forum/viewtopic.php?t=762&p=6728#p6728 <![CDATA[Re: Extension and Operation]]>
Sorry if I confused you about me using the Silicone sheet. No I do not intend using the sheet on the slip joints but I have used it elsewhere as gaskets.

As far as my philosophy is concerened the way that I see it, is that there are two sources of potential leaks;

1) Liquid - this is the distillate refluxing back down the column. By soldering the inner sleeve to the upper half of the joint the condensate will be directed well below the joint, to leak it would then have to turn round and run 4" vertically upwards, which I cannot see happening.

2) Vapour - This in theory will be as near to zero pressure as you can get. To escape it will have to travel upwards for 4" between the inner sleeve and the column then another 4" between column and the outer sleeve. If there are any leaks then I will put some sealant at the positions I have indicated on my sketch

http://www.stillsmart.co.uk/forum/viewtopic.php?f=15&t=733

Capt'n C, mentioned that he had used some food grade sealant, or you could use a four and water paste that a lot of people seem to prefer.

Time will tell if my joints leak, if they do then I will be asking you for advice on installing ferrules, so keep lots of notes.

Statistics: Posted by YHB — Tue Jan 03, 2012 3:45 pm


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2012-01-03T14:37:57+00:00 2012-01-03T14:37:57+00:00 http://www.stillsmart.co.uk/forum/viewtopic.php?t=762&p=6727#p6727 <![CDATA[Re: Extension and Operation]]>
My plan is to order the long ferrules and triclover clamps with a PTFE gasket to connect the pipes for the Boka build.

YHB, are you using the flat silicone sheet in combination with two hose clamps to seal each slip joint?

Statistics: Posted by Keystone — Tue Jan 03, 2012 2:37 pm


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2012-01-03T05:57:31+00:00 2012-01-03T05:57:31+00:00 http://www.stillsmart.co.uk/forum/viewtopic.php?t=762&p=6722#p6722 <![CDATA[Re: Extension and Operation]]>
Looking Forward to hearing the results!

Rubber from your bicycle tyre will degenenerate very quickly and is not recommended if it is in contact with the vapour stream - Silicone seems to be a better / safer alternative - I cut mine from my wifes baking sheet, which I get from Morrisons, the local supermarket for about 2.50 pounds. - That is OK if you want a flat sheet - but I also saw some silicone cup cake moulds that may be Ok if you are looking at rubber band type gaskets. Just cut the top and bottom out of these.

Image

I am due for a shopping trip tomorrow I will check up on the size.

Statistics: Posted by YHB — Tue Jan 03, 2012 5:57 am


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2012-01-02T23:15:49+00:00 2012-01-02T23:15:49+00:00 http://www.stillsmart.co.uk/forum/viewtopic.php?t=762&p=6721#p6721 <![CDATA[Extension and Operation]]>
To seal the pipe, teflon tape was wrapped around the pipe at either end to ensure a snug fit into each cap. Also, additional sealing was provided by two rubber gaskets cut from a bicycle inner tube rated for 1.75" to 2.35".

I will follow up with another post on operation. Generally, the boiler was powered up to 1125W for the hearts.

Statistics: Posted by Keystone — Mon Jan 02, 2012 11:15 pm


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