Should perhaps rename this thread 'Lessons learnt and learning'
Filled it up with 2 fermented peated malt washes popped power on as I loosely assembled the 6 to 4 inch reducer plus 4 to 2 inch torpedo SD with sight glass then column and Liebig just to get everything lined up. In no time at all had a foam puke.
Oops forgot to chuck some butter in obviously an immersion element is a bit fiercer than the flat bottomed T500
anyway got the power controller linked in and bugger no juice coming through.i had put a new longer lead on so internal look showed that the plug in connector on the regulator had come loose. Phew sorted
Any way as the moment approached it appeared I couldn't keep the puking down without getting any product
Ended up adding the 2 4" sight t sections (without the bubble plates) to give more head space still not good.eventually stuck in some copper mesh in the column to break up the bubble surges (I'd got this from distilling dominoes) and even let a bit of wash out to give more bubbling room and slowly bit by bit got going and eventually went on to do a normal run. Seemed a pretty good product too
What did I learn, do wrong and plan to do differently
Well because I wanted to do some other stuff this weekend I think I rushed the wash and it went in a bit cloudy and possibly still working a bit so more patience degassing and fining needed
Less wash in boiler and start with full column to give more head space.Actually having the 3 sight glasses simplified bubbling control
Try a bit distillers conditioner as well as butter
And I might put some of the copper wool around the heating element to try and disperses the heating effect
Would appreciate any thoughs, words of wisdom or comments no matter how scathing !Statistics: Posted by Admiral Toad — Fri Apr 03, 2015 4:56 pm
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