It's starting to look like a still...
Cutting the lid and silicone seal is done, just waiting on the loan of a large pipe wrench to finish the boiler end of things.
I did have doubts when I first saw the lid but I'm liking it now that the hole has been cut. The lip on the lid squishes up the silicone sheet a treat. So glad I went for new.
The 64mm hole for the tank connector went easier than I thought. Had to use 2 pieces of timber for support due to the dink in the middle of the lid. Loads of WD40 on the lid and a cheapo 4mm cobalt drill for a pilot hole, stopping every time the WD40 smoked, which was 5 to 10 seconds and then spraying some more on.
The holesaw arbor wouldn't fit in the cordless but just managed to fit in a single speed corded drill I had. Using my newly built power controller, I found the lowest setting it would run at and with lots more WD40, got stuck in.
Was a bit tedious having to keep stopping, no way I wanted the steel to work harden. When it did break through, the metal was only warm, not too hot to hold. About 20% of the hole needed to be deburred, 5 minutes with a file.
I removed the black gasket from the tank connector and cut out 2 extra gaskets from the silicone offcuts so as to match the thickness of the original gasket.
The 32mm clips are from the bay and are really strong. 2 clips 180 degrees apart is enough to let the (empty) boiler be picked up by the lids handle.
Next task is to rig up support for the column so that the boiler doesn't take the weight.


I did have doubts when I first saw the lid but I'm liking it now that the hole has been cut. The lip on the lid squishes up the silicone sheet a treat. So glad I went for new.
The 64mm hole for the tank connector went easier than I thought. Had to use 2 pieces of timber for support due to the dink in the middle of the lid. Loads of WD40 on the lid and a cheapo 4mm cobalt drill for a pilot hole, stopping every time the WD40 smoked, which was 5 to 10 seconds and then spraying some more on.
The holesaw arbor wouldn't fit in the cordless but just managed to fit in a single speed corded drill I had. Using my newly built power controller, I found the lowest setting it would run at and with lots more WD40, got stuck in.
Was a bit tedious having to keep stopping, no way I wanted the steel to work harden. When it did break through, the metal was only warm, not too hot to hold. About 20% of the hole needed to be deburred, 5 minutes with a file.
I removed the black gasket from the tank connector and cut out 2 extra gaskets from the silicone offcuts so as to match the thickness of the original gasket.
The 32mm clips are from the bay and are really strong. 2 clips 180 degrees apart is enough to let the (empty) boiler be picked up by the lids handle.
Next task is to rig up support for the column so that the boiler doesn't take the weight.
